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Exhibit A-Supplement 1 <br /> for the SGR soil borings. Additional cost are presented for this field work and report preparation work by <br /> SKS. <br /> Task 00200 Phase I Update—VE CR ABC <br /> Phase I update Roadway and Structures <br /> Roadway Geometry <br /> The original roadway geometry update was to include horizontal geometry tie in between the existing and <br /> proposed improvements of Brush College Road near the existing Norfolk Southern Railyard overpass. The <br /> previous south limit on BCR was station 50+00. This included profile modifications to tie into the existing <br /> underpass profile grade at approximately this station 50+00. During current design the limits had to be <br /> extended to the underpass about 340 feet. The new project limit south is station 46+59.44 and work will <br /> require tying into the existing RR viaduct. <br /> The IDS modifications in our current scope of work only included minor rework for the south tie in up to <br /> station 50+00 to be completed and submitted for D7 review. Through the Optimize Current Design task a <br /> shift in alignment was determined to be most beneficial for the project in saving construction cost on the <br /> bridge over the NS RR where a four-span structure was reduced to a two-span structure. This required more <br /> extensive rework of the IDS for IDOT review. During the review IDOT had additional comments on other <br /> legs of the roadway network which were previously approved in the phase I IDS process. This required <br /> additional IDS rework to gain approval. <br /> Multiple typical sections had to be developed for the sideroads to stay within existing ROW. Open ditch and <br /> curb and gutter sections were developed and reviewed to determine appropriate use by locations on the <br /> sideroads. <br /> With the extension south and added structural items(Cut Wall,L-Wall,and Structural Barrier)additional <br /> roadway support was used for providing wall profiles,typical sections, cross sections for design purposes, <br /> and design coordination. <br /> After 60%plan estimates were prepared efforts were completed towards cost saving measures on the project <br /> including possible elimination of the ICRR track shift. <br /> Additional hours are presented for IDS work,Typical section development,Horizontal and Vertical <br /> Geometry, Cross Section support and Cost Saving Measures. <br /> Revise Type, Size and Location(TSL)Plans <br /> Extension of the southern limit of the project required a cut wall TS&L be prepared. Quigg Engineering was <br /> assigned this work. The current project scope of work did not include walls other than MSE walls. Quigg <br /> Engineering was able to complete this scope change under the current hours assigned to them for TS&L <br /> work. No additional hours are presented for QEI TS&L work. <br /> WHKS is requesting hours for changes from MSE to Precast Modular Wall for the TS&L drawings and <br /> quantities on Wall 003. Additional hours are presented for WHKS TS&L work. <br /> Additional Scope 08-21-20 ExA S 1-2 <br />